Day 4:
Another up and down day! First we wanted to establish the final resting place for the 460. To do this we had to have a radiator and fan shroud to make sure the fan would center in the shroud. Since Walt had sent the radiator out for refurbishment, we had to retrieve it. Well, the new four-core was at Mike's when we arrived and we got two for one. We spent most of the morning getting the radiators in place. It turns out that the new four-core requires significantly more room and we had to relocate the A/C condensor forward of the core support. Then we could slide the new big mama into place. We made some studs out of bolts and nuts so that we could hang the new rad into place without struggling with it.
We found that we had no room for a fan!!! OK, so I had already been thinking ahead to electric fans so that would be the easy solution.
We finally established the final location of the motor. It turns out that the tranny mount and the passenger side motor mount seemed to be located correctly, but the driver's side had to be moved requiring new holes to be drilled in the frame. See Walt drill...
Oh, well, I guess the more holes the lighter the truck. Therefore it will go faster.
Once we got the LH mounts bolted in place, all was well with the world.
We turned on the polkas and Fred sang in Slovenian. We had the project by the tail on a downhill pull. My friend Jim stopped by and we celebrated.
We had to make a special carb adapter for this installation and celebration.
After the party, we soldiered on. The next step was the installation of the drive shafts with the new combo universal joint. To our astonishment, surprise and dismay, the front driveshaft ended 1.5 inches short of it's intended mark. The ZF S5-42's yoke stopped 1.5 inches shorter than the T19 before it. Our first plan was to find a longer driveshaft from a truck with the same tranny. That could be a needle in a haystack search. We also considered having the current driveshaft lengthened. After a lot of noodlin', we decided to consider moving the motor back 1.5 inches. We looked and measured and looked and measured and decided it was worth a try. It will mean pulling the motor again to drill new frame holes but again, this will lighten the truck and make it run faster so we figgered it was worth it. This will also give us more room between the water pump and radiator and has the further benefit of cost savings by not having to spend money on a new or custom driveshaft.
Maybe it will work....tune in tomorrow.....